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Horizontal Stabilizer

Date Hours  
2/11/2005 4.5 The empennage kit arrived this afternoon. Christine called me at work with the news. I went home soon afterward. I first inventoried the two boxes. Everything was there. With some of the extra skin material I practiced drilling holes, dimpling and riveting. I then Alumipreped and Alodined some of it to see what it would look like. I tried to get comfortable with the tools and procedures.

I couldn't resist. I Clecoed the horizontal stab skins onto the rear spar. I took this apart and then started on the first step - break the edges of the rear spar stiffener. I used the Scotch Brite wheel on my bench grinder to do this.

2/12/2005 8.5 First thing I realized was that I only have carpentry files so I made a quick trip to Home Depot to buy a metal bastard file. I bought the coarsest they had but it wasn't really up to the task. It took me a couple of hours to do all of the filing. I then put it under the Scotch Brite wheel. It turned out really nice. I then match drilled the holes in the rear spar as per the instructions.

I then put together the center elevator bearing hinge. I match drilled the holes on the drill press and then primed the bearing. The advice in the construction manual to have a can of self etching primer is good.  I went to the trouble Alumiprep, Alodine and prime it all because  I didn't have a spray can of primer and I wanted to go through the process to spray it on anyway. When it dried I riveted it together. This was my first real riveting job (other than practicing with scrap).

After more match drilling, I then moved on to the front spar. More match drilling on it and then I shaped the re-enforcing bars. Again I used a not-course-enough file and spent hours getting it to look right.

2/13/2005 7.0 My knuckles are still sore from all of that filing yesterday. I started today by bending the two front spar re-enforcing bars 6 degrees. I mounted them in a vise between wood blocks and used a mallet to bend them.

Next I notched the two inside front ribs to fit around the re-enforcing bars. The metal shears worked well for this for a rough cut. First I drilled a hole where I had to make a 90. I then filed (again, aaargh) them down smooth and then put them under the Scotch Brite wheel.

I then fluted some of the ribs using fluting pliers. It is amazing how that works. The ribs were all little bent from the manufacturing process and just by bending (fluting) the flange part straightens it out perfectly. I then Clecoed the spras and ribs together and drilled some holes.

 

I took it all apart, cleaned the holes and put it all back together. This time I Clecoed on the skin on the left side. I match drilled the holes on the inside rib and the inboard part of the spar.

 

2/14/2005 4.1 I flew to Weiser Airpark today to put up for-sale flyers for the Warrior. I found out that one of the schools has a Citabria. I should be able to get some time on it to get my tail dragger endorsement and do some basic aerobatics.

The yoke for the pneumatic squeezer came in today. I put it together and practiced dimpling and riveting some scrap. The scrap is now scrapier.

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I finished drilling the front inside rib and then removed the Clecos in the left stabilizer. I then drilled and did everything I did to the right stabilizer as I did to the left one. The picture above is of the right stabilizer flipped upside down.

It wasn't easy to drill the holes that attach the inside rib flanges to the front spar. I used a long drill it which I bent slightly as it turned to try to get it to be normal to the spar. Riveting these is going to be interesting.

I also didn't notice that the front two holes in the outer spar on the left stabilizer need to be drilled. I need to Cleco most of it together again to do this Aargh! When that is done, it will be time to debur the holes, have one last shot at breaking edges and then Alumiprep, Alodine and prime everything. I still don't have a plan for containing the giant cloud of primer that will surely result.

2/15/2005 3.2 This afternoon I went to Home Depot to price supplies needed to make a paint booth.

I put the right stabilizer back together with Clecos because I was worried about the hole lining up between the skin, re-enforcing bar and middle spar. When I was taking out the Clecos last night I noticed that it wasn't lined up by almost a full diameter. When I put the Clecos in tonight, it was within about 1/4 of a diameter and the Cleco went right in. Panic over nothing. I took it apart and Clecos the left stabilizer back together. I needed to do this to drill the two holes I missed last night.

I removed the plastic on the inside of the skins, broke the edges and deburred the holes. Everything is ready for Alumiprep and Alodine.

The first picture below is of the front web of the middle right spar inside of the innermost rib. Hopeful it shows how little clearance there is for drilling and riveting.. The second picture is of the same but from the side.

The third picture shows the outside of the outside right rib. The fourth one is of the inside of the right stabilizer as viewed from the inside rib. The multiple reflections really make it confusing to look at. There are two Clecos on the top - the rest are reflections. The dotted lines going up and down are flutes in the middle rib.

After I finished with this, I practiced dimpling and squeezing rivets with my pneumatic squeezer.

2/16/2005 0 No progress today. I again practiced dimpling and riveting with my pneumatic squeezer. I think I have the hang of it. I tried dimpling both with the blue plastic in place and with it removed. The end result looks a lot nicer when done with the plastic in place. The dimples look identical in both cases except that there are no tool marks with the plastic.

 

At lunch I went to Harbor Freight on a recon mission. I bought a HVLP mini spray gun. HVLP means high volume low pressure. It is supposed to put more paint on the surface and less generating a friendly neighborhood cumulonimbus. It is supposed to do a better job too. I'll soon find out.

2/17/2005 5.5 Tonight I dimpled one stabilizer skin, applied Alumiprep, washed it off, applied Alodine and wiped it off. The end result was spotty as you can see below. Maybe Maybe I didn't leave the Alodine on there long enough or perhaps it became diluted in some areas because opf the water still on the skin. I might re-do it tomorrow.

One problem I had was the front middle rivets. My C-Frame bumps up against the skin where it can barely get to the second rivet but certainly not the first. There are probably several ways to do this but I chose to drill a hole on one of the rough sides of my bucking bar so that the die could fit into it. It worked just fine.

The C-Frame scratches the aluminum. I put it on top of a towel but that didn't help a whole lot.

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On the third to last dimple on the right spar, I manager to poke a hole in the flange part of the rib with the pneumatic dimpler. It went through it like butter. I started to try to "fix" it but I decided against it. This was a real bummer. I turned in for the night.

I think part of the problem is that I was tired after working a full work day and then almost 6 hours on this.

2/18/2005 4.7 This morning I planned to call Van's or the local EAA chapter for some advice on what to do about the spar. I first checked on Van's web site and found out the spar just costs $18. Case closed. No need for expert advice on a repair. I re-ordered the spar.

I thought my idea about the bucking bar was original but I found it in the Van's manual. I had read it before but apparently it was retained by only 1 or 2 of my neurons.

Tonight I Alodined the skin again and this time put it on thicker and made sure it was on for the full amount of time. It turned out a lot better (see below). I finished dimpling and then I etched and Alodined the rest of the stabilizer parts.

I plan to continue with the stabilizer with the spar with 1 extra hole up until it is time to rivet it in. The new spar should be in way before then and after preparation, I'll make the substitution.

 

I am ready to prime.

2/19/2005 5.8 Christine and I went to Lowe's and bought a bunch of PVC and fittings. We both built the very temporary paint booth you see below. Lowe's didn't have all of the fittings we needed so I substituted with duke tape.

 

I primed all of the stabilizer parts. I used 600mL of Akzo to cover everything with a fairly light coat. I know it's and eye sore so please excuse the picture of me. I will someday need to prove to the FAA that I did all of this.

Lessons:

  • The paint boot isn't necessary with the HVLP spray gun. There is very little paint mist.
  • The fumes are strong. I wore all of the protective garb with a mask with filters and I still breathed in some of that stuff. Since there is very little mist with the HVLP gun, next time I'll paint out in the open.
  • Before the 30 minute "induction" period,  some acetone needs to be shot through the gun to keep it from getting clogged.
  • Having the parts hanging from wires is OK since the gun doesn't really blow them around. I had them laying down on coat hangers (our chicken wire substitute) which lead to inevitable touch marks when I had to turn them over.

I don't think it is the greatest paint job in the world (due to the touch marks) but I think it is good enough.

2/20/2005 9.4 I riveted the re-enforcement and splice bars to the back of both spars. I used the squeezer as much as possible to keep the noise down. The neighbors are having a back yard party. I had a very hard time riveting the outboard hinge brackets. The rivets called for in the plans, AN470AD4-7, seemed too long. I messed two up really bad and had to drill them out.

 
I didn't rivet in one of the rear spar halves, which I have decided to replace.

I went flying (to show the Warrior to a prospective buyer) and then came back and resumed assembly of the left stabilizer. I riveted the front middle rib onto the skin on both the front and back sides. I couldn't get my hand in to buck the rivets but Christine came to the rescue. All except one turned out great. I didn't push down on the rivet gun enough so the rivet was not flush. I drilled it out and we did it again. This time it turned out perfect.

I am getting to be pretty good at drilling out rivets Unfortunately it highlights my my lack of skill in other areas.

Text Box: Blind rivets
I then blind riveted the front and back middle ribs to the middle spar with blind rivets.  The occasional gray in these pictures is of self etching primer. Whenever I manage to ding the original primer, I give it a little shot of this stuff to keep it protected.

 

Lessons Learned Today:

  • A 1 lb bucking bar is not enough for AD4 rivets. My arm is still shaking.
  • Think before riveting or else you might have to drill it out (like I did).
2/21/2005 3.5 I finished cutting off strips of the blue plastic skin protector from around the rivets. I riveted the skin to the middle spar and the back middle rib. I then moved on to the right stabilizer. I riveted the front middle rib to the skin, put it around the middle spar and blind riveted the rear middle rib to the middle spar and the front middle rib.

Out of all of these rivets, I only had to drill one out. This one was because I riveted one place with the plastic still over the hole. Aaargh. Since I am no expert, I checked ALL rivets with my handy rivet gauge. I had to pound some more on about a half a dozen of them.

I am finding that very little pressure to the rivet gun is working out best for me. About 25 PSI seems right for these AN426AD3-3.5 rivets.

2/23/2005 3.1 I finished riveting the middle rib and spar on the other stabilizer. I then removed 4 rivets I had put into the middle of the front spar by mistake. I then touched up with primer a few areas I had dinged with the bucking bar.

Text Box: Rivets were put in here by mistake. These are for attaching the stabilizer to the fuselage.

The primer is tenacious. I managed not to scratch the inside skins even though I accidentally let the bucking bar bump against it several times while riveting.

I don't think there's anything else to do on the horizontal stab until the replacement rear spar comes in.. I am going to work on the Vertical stab. for now.

3/2/2005 3.5 The replacement horizontal stab came in today. I did a lot. I drilled, deburred, cleaned the edges, dimpled, Alumipreped, Alodined and primed it.
3/4/2005 3.1 Tonight I riveted the rear spar together and riveted the outside of the skin to the inner and outer ribs and rear spar. I bolted on the center hinge bracket and torqued the bolts to 22.5 in/lbs.

3/5/2005 3.7 I finished riveting the horizontal stabilizer! I peeled off the plastic since Van's says it might stick too well if left on for too long. I loosely taped paper around it and stored it on a high shelf in the garage.

5/7/2005 2.4 I worked on the fiberglass ends. I trimmed the right elevator end to the right size. I then made a small block of foam and put it into the horizontal stab tip, fiberglassed the back and micro-ballooned  the part you can see. I set it on waxed paper which I hope will leave a very smooth surface.
5/8/2005 2.0 I did the same to the left tip. I filled some pin holes in the right tip.
5/9/2005 3.1

I made and primed an aluminum strip to back up the rivets. I then countersunk the skins and popped the rivets into place. Yes, I de-burred and primed the metal parts.

Text Box: These weren't easy but I had been warned.
Text Box: Hmmh. Nice rivets on the top and bottom sides thanks to Christine..

Total Time: 74,7

email: Luis Luciani